08/15/2022
The initial work on Nico's truck has been completed and it was delivered on Saturday afternoon (8/13/22.) We took it out for a ride together and in Nico's words he is “stoked!” Along the way various motorists we encountered gave us the thumbs up and cool truck call-outs as we drove around Watertown. Lets back up a step and consider how we got to the point where Nico got his truck back …... The initial estimate contained three parts, a complete rebuild of the brake system, the only previous work being a new brake line from the front to the rear axle. Part two was a minor tune-up along with a compression test to ensure the basic engine is in a satisfactory condition (it was fine.) Part three was basic maintenance including changing the engine oil/filter, and the oil in the transmission and transfer case and both axles. There were discussions about the wiring …. it was / is pretty chaotic and the temperature gauge was not operating. So the first step involved taking the brakes apart and ordering parts. Two sets of front brake hoses, two sets of front wheel bearing seals, five front wheel cylinders, three sets of rear axle seals along with all the parts that actually fit the first time (the rear wheel wheel cylinders, the rear brake hose and the front and rear brake shoes fit the first time!) Thanks to Larry and Ty at Advance, Brad and Zack at Autozone and Randy at Standard/Napa. As the job progressed I found out a lot about 1971 International 1310 / One-ton pick up trucks. This one was originally specially ordered by the Milton Vermont Fire Department with a Two-ton Dana 70 HD rear axle. Once the brakes and maintenance were completed the tune-up caused some complications. At first the spark was weak so we upgraded and installed points, condenser, coil, cap and rotor. I drove it with Nico and it wouldn't accelerate properly so further work was required. When I measured the running voltage at the positive side of the coil and it was at full battery voltage instead of dropping down to six volts. The wiring diagram indicated a resistor wire was originally part of the factory wiring but it was gone. A new replacement ballast resistor from a 60's Mopar was purchased and installed and the ignition problem was resolved. Lastly the gauge pods were removed from the dash and the corrosion was cleaned off the printed circuit going to the temperature gauge. Nico is planning on driving the truck as much as possible and enjoy his new / old truck!